I have a compressor and before I changed my oil it used to fill my pcp all the way up to 4500 psi and after I made the oil change it takes forever to fill and it fills only to 4000 psi if I’m lucky
Yesterday I managed to seize that piston rod. Oh well, I have one new full assembly (first and second stage) on order from aliexpress, ETA 2 weeks.It just happened to me today... ...I shall have one complete piston + headset in spare, but I will be ordering a full kit from aliexpress soon.
Look hard at your check valves, the ones connected your SS lines. There easy to get to, so look for corrosion or chipped O-rings or bad Dowty washer, Mine was just cleaned...Already tried the soap and nothing happened, and something I’ve notice is that if I charge my pcp and leave it without releasing the pressure on the line it starts dropping by it self slowly but I can’t find the leak.
the dipper is on the bottom of the piston rod (not shown in picture)....I notice there is no “dipper” on the bottom of the crank, did it break off, or did it not have one?
What brand oil? Mine blackens any oil used after used but still making good pressure... Thx.Piston rod seized, this is a second time. I tried to sandpaper down the surface but looks like didn't help.
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Have a spare pump for parts whenever needed, any idea how to take this crank shaft out without some specialty tool? The screw I brake loose but cannot pull it out.
I would have a good use for it now
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The next option is get a new compressor... but closest I can reach is a Tuxing from amazon...
Check the pressure gauge, that's the first thing to fail on my yong hengs.Already tried the soap and nothing happened, and something I’ve notice is that if I charge my pcp and leave it without releasing the pressure on the line it starts dropping by it self slowly but I can’t find the leak.
I have a yong hang 4500 psi compressor sold by VEVOR. Bought it not yet two months ago. It’s not filling my 4500 psi air tank. The compressor shuts down at 4000 psi and lower when I drained the air and restarted after pushing in the breaker on the back.
Leak test already done.
Even with a dead head , it looses pressure.
I’m guessing piston rings !
I’ve contacted custom service.
I shouldn’t have to repair this with less than 4 hours run time.
It worked great at first , filling my pcp rifle from 0 to 3625 psi in 5 minutes. Then I bought a 4.5 L 4500 psi air tank. Filled to 2000 psi in 15 minutes before letting it cool down . Then filled to 3500 in 30 minutes before cooling it down. Then the trouble started!
It progressively got slower and slower.
When I got it , the big brown truck had it standing on it’s end. Oil leaked out inside the box.
The breather tube was already installed and from standing on it’s end , cracked the breather tube down at the threads.
I’m either unlucky getting a bad unit or it was a return and somehow I wound up with it!
I’m frustrated to say the least…