I do a lot of modifications to PCP rifles. And the following I will be presenting to you should NOT BE ATTEMPTED unless you have thorough knowledge of how pcp's work, inside and out, but mostly inside. The following was done with VERY limited set of tools : drill, dremel, clamps, peek/delrin rod, brass/copper washer, hss 1/8 drill blank, jb weld, sand paper.
What separates my arrangement from most is the micro valve stem and reduced seat, thanks to it, I am allowed a smaller poppet OD, the latter 2 GREATLY reduce the requirements to open the valve. A stock valve stem would require a much larger valve seat/throat + poppet OD which in turn would make the valve harder to open. The last major change that reduces forces required to open the valve is higher quality material over stock with less young modulus ie: peek poppet and brass or copper seat. I'd love to try something MUCH more harder for a valve seat in the future, maybe if/when this valve ever fails.
Rifle:
.25 Cal Marauder
Valve specs:
.2275" (.234" x .221") Valve exit port and Transfer port (91% of bore)
.225" Barrel port (.212" x .238") (90% of bore)
.237" Valve seat (over 5% greater cross sectional area than forward porting to compensate for flow loss across seat)
.275" Peek Poppet (.19" sealing margin)
.04" HSS Micro Valve Stem (ran one for a year to test, now testing further, may increase 10-20% if one fails in the future..)
Gen 1 style bolt probe modified for the above porting.
Valve hogged .5" down to valve seat (stock = .42")
Old valve seat sanded down/removed
Stock hammer travel: .75"~
Modded hammer travel .88"~
47.5 Gr MDS hammer + 7.7 lb spring
As you see from the above specs, I stretched just about every single one of them to their max. Other rifles may be different but the Marauder is mostly limited to the flat spot on the barrel being .285" which would allow a transfer port of .285" with .02" walls and .245" porting which equates roughly to .245 x .21 = .2275"....going further risks damage to pellets, you can go to .23" but that is really about it without creating a new bigger flat spot and that I am not equipped to do, and even if I were I find the methods/techniques and my outcome acceptable enough.
Pic1: Here I admittedly messed up and drilled out the valve exit before the throat, which reduced a ton of metal at the top of the valve and caused my drill bit to wander when drilling the throat...very important to always drill out the throat first or use a really good vice + drill press but I do all by hand so, the original idea was to leave the original seat intact and attempt the crazy over 90% porting, but when life gives you lemons you make lemon aid. Next to the valve are the copper washers I picked up to 'Repair' the seat, I use this method to move the seat forward on my other valve anyhow..I really wanted to do over .225" porting without having to move the seat forward, which I know is possible but requires a 90 degree valve exit hole opposed to 45-65 degree, on top of quite a few other tricks and snags to avoid...maybe another day I will try again knowing what I know.

Pic2: Is just a picture showing the width of the valve exit port, as I stated earlier it is .234" wide (side to side) by .221" (front to back). Prior to breaking through the stock seat I planned on .24x.21.

Pic3: Peek poppet, micro valve stem and valve. Lots of markings on the valve as I just vice gripped it when hogging out and various other things and occasionally it would catch and spin..no functional damage only cosmetic that no one ever sees. Can also note the valve was shortened .1" in this pic. I also reduce the poppet sticking out of the stem over factory, which is .25" from factory and .185" in mine...which increases the hammer travel ever so slightly on top of the .1 I remove from back of valve.

Pic4: custom transfer port that matches both valve exit + barrel port. I hand make this starting with .3125" delrin taking it to .285"~ OD which allows up to .245"~ porting. I carefully match the porting and index the TP..definitely the most time consuming part of the whole job since matching oblong ports on TWO sides is a bit challenging, especially when striving for as near as perfect as one can do. The tp required me to drill through my air tube and receiver to allow the .285" Tp to slide in/out easily. The barrel port flat spot is .285"~ od and the valves is .3"~, while the receiver+air tube holes are closer to .26-.27.

Pic5: here is what it can do on just 7.7 lbs of hammer spring...at .6 pre-load which is not quite coil bound so there is more...and no this is NOT the valves PLATEAU. That would be roughly 900 FPS @ the regulated 2000 psi its currently at...this was with a 33.95 MK ll (56 FPE)


Pic7+8: Here is how I make my micro valve stem, chucked up in a drill with a dremel and cut off wheel I carefully remove area between the tape marks until I am roughly to .005" within spec where I then chuck the valve stem into the dremel and use sand paper to get a fine polished finish


Pic9: A graph of my tunes + cocking forces for said tunes..

That about sums up how to achieve over 90% bore porting with a modified OEM valve...by hand! The margins are small, and going even larger in ports without extensive modifications they become even smaller. Without creating new flat spots on valve + barrel, the safest I could personally take a .25 cal marauder is roughly .23"...which I came close enough to, when doing such by hand I like to leave a little extra margin for any mistakes I may make, .2275" valve and .225" barrel are those margins for me. Unfortunately I didn't snap pics of my poppet head making process but as you see from its pic, I think it came out well for being done by hand! I use the same method as the valve stem, for the most part, with a few techniques added to keep everything concentric.
And yes I have a marauder, with a 19.5" barrel, that makes 60 FPE (900 FPS 33.95 JSB) at just 138 bar...2000 psi. The valve seat is currently adhered using JB weld, where I ideally would use a 1 part epoxy that retains a LITTLE flex..and may move to such in the future if and when the current jb weld fails. I stress tested BOTH using a 98 gram hammer and fully preloaded 7.7 spring to wack the heck out of the valve, and it survived multiple. Also the micro stem reduced to .04 was only reduced by a factor equal to the force reduction required to unseat/open the valve PLUS the reduced energy required to open it...its quite the balance to make sure failure isn't inevitable.
FWIW there are people with 'balanced' valves that use heavier hammers and springs...so to achieve the above using a conventional valve is quite impressive...as you can see this project didn't quite go as planned, but failure or mistakes shouldn't keep anyone from pressing forward and striving for success! My marauder when stock came with a 8.5-9lb spring shooting 38-40 fpe @ 3k psi with a 78 gram hammer. I have since regulated and modified the valve so it does 60 fpe at 1000 less psi (2k) with 40% less hammer and 20% less spring...using the SAME valve with different specs.
Cost of modifications:
Peek + Delrin rod = 15$ (enough to attempt nearly 20 tp's and 20 poppet heads)
Copper washer = 75 cents (brass much cheaper, the #12 size I would need for brass isn't available locally)
Hss drill blank = 5$ ( I got 3 for 5 which in turn makes 6 stems)
Time invloved: Lots, so if you over value your time when tinkering with a hobby, then leave it to the pros
-Matt
What separates my arrangement from most is the micro valve stem and reduced seat, thanks to it, I am allowed a smaller poppet OD, the latter 2 GREATLY reduce the requirements to open the valve. A stock valve stem would require a much larger valve seat/throat + poppet OD which in turn would make the valve harder to open. The last major change that reduces forces required to open the valve is higher quality material over stock with less young modulus ie: peek poppet and brass or copper seat. I'd love to try something MUCH more harder for a valve seat in the future, maybe if/when this valve ever fails.
Rifle:
.25 Cal Marauder
Valve specs:
.2275" (.234" x .221") Valve exit port and Transfer port (91% of bore)
.225" Barrel port (.212" x .238") (90% of bore)
.237" Valve seat (over 5% greater cross sectional area than forward porting to compensate for flow loss across seat)
.275" Peek Poppet (.19" sealing margin)
.04" HSS Micro Valve Stem (ran one for a year to test, now testing further, may increase 10-20% if one fails in the future..)
Gen 1 style bolt probe modified for the above porting.
Valve hogged .5" down to valve seat (stock = .42")
Old valve seat sanded down/removed
Stock hammer travel: .75"~
Modded hammer travel .88"~
47.5 Gr MDS hammer + 7.7 lb spring
As you see from the above specs, I stretched just about every single one of them to their max. Other rifles may be different but the Marauder is mostly limited to the flat spot on the barrel being .285" which would allow a transfer port of .285" with .02" walls and .245" porting which equates roughly to .245 x .21 = .2275"....going further risks damage to pellets, you can go to .23" but that is really about it without creating a new bigger flat spot and that I am not equipped to do, and even if I were I find the methods/techniques and my outcome acceptable enough.
Pic1: Here I admittedly messed up and drilled out the valve exit before the throat, which reduced a ton of metal at the top of the valve and caused my drill bit to wander when drilling the throat...very important to always drill out the throat first or use a really good vice + drill press but I do all by hand so, the original idea was to leave the original seat intact and attempt the crazy over 90% porting, but when life gives you lemons you make lemon aid. Next to the valve are the copper washers I picked up to 'Repair' the seat, I use this method to move the seat forward on my other valve anyhow..I really wanted to do over .225" porting without having to move the seat forward, which I know is possible but requires a 90 degree valve exit hole opposed to 45-65 degree, on top of quite a few other tricks and snags to avoid...maybe another day I will try again knowing what I know.

Pic2: Is just a picture showing the width of the valve exit port, as I stated earlier it is .234" wide (side to side) by .221" (front to back). Prior to breaking through the stock seat I planned on .24x.21.

Pic3: Peek poppet, micro valve stem and valve. Lots of markings on the valve as I just vice gripped it when hogging out and various other things and occasionally it would catch and spin..no functional damage only cosmetic that no one ever sees. Can also note the valve was shortened .1" in this pic. I also reduce the poppet sticking out of the stem over factory, which is .25" from factory and .185" in mine...which increases the hammer travel ever so slightly on top of the .1 I remove from back of valve.

Pic4: custom transfer port that matches both valve exit + barrel port. I hand make this starting with .3125" delrin taking it to .285"~ OD which allows up to .245"~ porting. I carefully match the porting and index the TP..definitely the most time consuming part of the whole job since matching oblong ports on TWO sides is a bit challenging, especially when striving for as near as perfect as one can do. The tp required me to drill through my air tube and receiver to allow the .285" Tp to slide in/out easily. The barrel port flat spot is .285"~ od and the valves is .3"~, while the receiver+air tube holes are closer to .26-.27.

Pic5: here is what it can do on just 7.7 lbs of hammer spring...at .6 pre-load which is not quite coil bound so there is more...and no this is NOT the valves PLATEAU. That would be roughly 900 FPS @ the regulated 2000 psi its currently at...this was with a 33.95 MK ll (56 FPE)


Pic7+8: Here is how I make my micro valve stem, chucked up in a drill with a dremel and cut off wheel I carefully remove area between the tape marks until I am roughly to .005" within spec where I then chuck the valve stem into the dremel and use sand paper to get a fine polished finish


Pic9: A graph of my tunes + cocking forces for said tunes..

That about sums up how to achieve over 90% bore porting with a modified OEM valve...by hand! The margins are small, and going even larger in ports without extensive modifications they become even smaller. Without creating new flat spots on valve + barrel, the safest I could personally take a .25 cal marauder is roughly .23"...which I came close enough to, when doing such by hand I like to leave a little extra margin for any mistakes I may make, .2275" valve and .225" barrel are those margins for me. Unfortunately I didn't snap pics of my poppet head making process but as you see from its pic, I think it came out well for being done by hand! I use the same method as the valve stem, for the most part, with a few techniques added to keep everything concentric.
And yes I have a marauder, with a 19.5" barrel, that makes 60 FPE (900 FPS 33.95 JSB) at just 138 bar...2000 psi. The valve seat is currently adhered using JB weld, where I ideally would use a 1 part epoxy that retains a LITTLE flex..and may move to such in the future if and when the current jb weld fails. I stress tested BOTH using a 98 gram hammer and fully preloaded 7.7 spring to wack the heck out of the valve, and it survived multiple. Also the micro stem reduced to .04 was only reduced by a factor equal to the force reduction required to unseat/open the valve PLUS the reduced energy required to open it...its quite the balance to make sure failure isn't inevitable.
FWIW there are people with 'balanced' valves that use heavier hammers and springs...so to achieve the above using a conventional valve is quite impressive...as you can see this project didn't quite go as planned, but failure or mistakes shouldn't keep anyone from pressing forward and striving for success! My marauder when stock came with a 8.5-9lb spring shooting 38-40 fpe @ 3k psi with a 78 gram hammer. I have since regulated and modified the valve so it does 60 fpe at 1000 less psi (2k) with 40% less hammer and 20% less spring...using the SAME valve with different specs.
Cost of modifications:
Peek + Delrin rod = 15$ (enough to attempt nearly 20 tp's and 20 poppet heads)
Copper washer = 75 cents (brass much cheaper, the #12 size I would need for brass isn't available locally)
Hss drill blank = 5$ ( I got 3 for 5 which in turn makes 6 stems)
Time invloved: Lots, so if you over value your time when tinkering with a hobby, then leave it to the pros
-Matt